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COMMONWEALTH OF PENNSYLVANIA

DEPARTMENT OF ENVIRONMENTAL

PROTECTION

SURFACE INSPECTION REPORT

5500-FM-OG0114(M) 06/2021

v1.2.13

DEP USE

ONLY

Inspection Record

No.

3586521

Complaint Record

No.

373528

Enforcement Record

No.

DEP Office Knox Oil & Gas Office Inspection Type PF

Address P.O. Box 669 Permit or Reg. # 063-27569

Addr Cont Knox, PA 16232-0669 ESCGP # ----

Oper. Name DAKOTA OIL & GAS CO Site # 121311

Oper. Address

6608 RTE 22

DELMONT, PA 15626-2408 Project # 063-27569

Resp. Official Name Marc Jacobs Farm Name & Well # KENNETH D MUMAU ET UX 1 WELL

Resp. Official Phone 412 389-5253 Other Info ----

Latitude 40.756497 Longitude -78.942652

County Indiana Municipality Grant Township

Inspection Code INCDT - Incident- Response to Accident or

Event Facility Single-Well Pad

Permits/Auths Well Permit Site Phase Restored/Prod

Well Info Conventional

Well Kind &

Description

Vertical Well

Stream Class

* HQ-CWF - High Quality Waters - Cold Water Fishes

Watershed

17D - Mahoning Creek

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COMMONWEALTH OF PENNSYLVANIA

DEPARTMENT OF ENVIRONMENTAL

PROTECTION

SURFACE INSPECTION REPORT

5500-FM-OG0114(M) 06/2021

v1.2.13

DEP USE

ONLY

Inspection Record

No.

3586521

Complaint Record

No.

373528

Enforcement Record

No.

GENERAL COMMENTS

On 7/18/23 at 0900 hrs., I conducted an inspection of Dakota Oil & Gas Co.'s Kenneth D Mumau et ux 1 well (API 063-27569)

in Grant Twp., Indiana Co. in response to a reported production fluid release. On 7/13/23, the operator reported a release of

approximately 5 barrels of production fluid onto the ground, due to a mowing incident by the landowner. Excavation of the

release area was conducted on 7/14/23. Photos of the release area and initial excavation were provided to the Department via

email, and have been uploaded to eFacts. Impacted material is staged onsite on 20 mil plastic liner. The excavation area and

impacted soil were also covered with 20 mil liner. Soil conductivity screening of the excavation is to occur later today, 7/18/23,

and additional excavation will be conducted as needed.

The production fluid tank was emptied and removed from the site prior to inspection. The well is equipped for production. A well

tag is affixed to the well head. The operator has been reminded that a site ID sign with the operator’s name, address, phone

number, and well permit number should be re-posted once the brine tank is replaced.

Violations of 78.57(a), SWMA 610(1), SWMA 301, and SWMA 302(A) are cited for the release of production fluids from the

tank onto the ground. The violations will be resolved upon remediation of the site and attainment of an Act 2 standard. Please

refer to page 3 of this Notice of Violation regarding a written response describing how you intend to remediate the release and

demonstrate attainment of an Act 2 standard.

REMARKS / VIOLATIONS

Category Sub-Category Inspection Remarks / Violations / Violation Remarks I R V

Spills & Releases 1: Reporting /

Remediating

Releases:

Reporting /

Remediating

Releases

Inspection Remark: On 7/13/23, the operator reported a release of

approximately 5 barrels of production fluid onto the ground.

Excavation of the release area was conducted on 7/14/23. Impacted

material is staged onsite on 20 mil plastic liner. The excavation area

and impacted soil were also covered with 20 mil liner. Soil

conductivity screening of the excavation is to occur later today,

7/18/23, and additional excavation will be conducted as needed.

☑ ☑ ⬜

Waste Control &

Disposal

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COMMONWEALTH OF PENNSYLVANIA

DEPARTMENT OF ENVIRONMENTAL

PROTECTION

SURFACE INSPECTION REPORT

5500-FM-OG0114(M) 06/2021

v1.2.13

DEP USE

ONLY

Inspection Record

No.

3586521

Complaint Record

No.

373528

Enforcement Record

No.

1: Production

Fluids Control &

Storage :

Production Fluids

Control & Storage

Inspection Remark: A release of approximately 5 barrels of

production fluid from an on-site tank to the ground was reported on

7/13/23. The production fluid tank was emptied and removed from the

site prior to inspection.

☑ ☑ ☑

NEW Violation:78.57(a) - CONTROL, STORAGE AND DISPOSAL OF

PRODUCTION FLUIDS - Operator failed to collect the brine and

other fluids produced during operation, service and plugging of the

well in a tank, pit or a series of pits or tanks, or other device approved

by the Department or Operator discharged brine or other fluids on or

into the ground or into waters of the Commonwealth.

Violation Date: 2023-07-18

Violation Remarks: A release of approximately 5 barrels of

production fluid from an on-site tank to the ground was reported on

7/13/23.

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